Quantcast
Channel: ArduCopter - ArduPilot Discourse
Viewing all articles
Browse latest Browse all 21359

Autotune PID terriblly bad--copter 3.3

$
0
0

@farstein wrote:

Firmware :copter 3.3 hex;
980mm;
Weight:about 6kg,with Anti-Vibration Platform like below ;

I landed the copter and save the pid after it was sucessfully autotuned in a good weather.Then I refly my copter, it vibrate so heavily that I almost can't control it. It seems that it fly well before I first landed the copter.

Is the autotune imperfect at present? Or the autotune is not recommend?

I'm sorry the log was lost because the test was done months ago .

Posts: 5

Participants: 3

Read full topic


Viewing all articles
Browse latest Browse all 21359

Trending Articles